Skip to content
Neundorfer 50 Year Anniversary Logo
Home Insights Maintaining Operations after Equipment Damage

Maintaining Operations after Equipment Damage

Summary

When an industrial steam generator experienced a major process upset and damaged their electrostatic precipitator (ESP), they could not shut down to make the necessary repairs. Neundorfer was able to optimize the performance of the precipitator which allowed the plant to find the production point that would allow the equipment to stay in compliance until the regularly scheduled shutdown.

Full Story

Many industrial processes require steam for the manufacturing of their product.  In many cases fossil fueled or biomass boilers are used to generate steam for their process.  This plant used coal-fired boilers to generate their steam.  After a lengthy maintenance outage, one of the boilers experienced an upset that damaged the internals of their ESP during a high temperature excursion.  This resulted in warping the internal collecting plates, creating close clearances that drove voltage levels very low with high sparking.  Maintaining production levels was critical and losing this source of steam production would have had a negative impact.

Neundorfer evaluated the operation of the boiler, data from recent testing, and data on the operation of the ESP.  It was concluded the boiler could run at 70% of maximum capacity and meet emission limits if the ESP operation was tuned.

Neundorfer arrived onsite, and after the adjustments to the precipitator were made, the performance allowed the boiler to meet Industrial Boiler MACT emission limits.  This meant the plant could stay in compliance until the regularly scheduled shutdown.  The second part of the strategy was to develop a cost-effective plan to make the repairs at the next scheduled shutdown.

Planning for the repairs began immediately.  Although changes to boiler operations were made to minimize the risk of a future incident, repairing the damaged internals with components less susceptible to heat excursions was part of the plan.  The most obvious damage was targeted, but it was also decided to repair the second and third priority items as the operating data indicated future risk to performance if they were not addressed.

The project is underway, but implementing the repair will return the boiler to full steam production with significant emissions compliance margin for the future.

Ready to Talk?

Get started working with Neundorfer today & see how we can assist your company.

Contact Us

From Our Optimized Insights

Latest Insights

  • News Article

    A Message from Steve, CEO

    We want to express our appreciation for our valued customers and the dedicated team members who continue to make Neundorfer a success in our industry.

  • Case Study

    Major Steel Producer Improves ESP Performance with Neundorfer without any Shutdown Days

    A large, integrated steel producer wanted to reduce the unplanned production stops on their BOF– a result of issues with their ESP. Neundorfer provided an integrated solution that was implemented while maintaining consistent production!

  • News Article

    POS Updates & Releases

    An upcoming feature will introduce a new button to the Utilities screen, which will allow the user to generate a history snapshot file with a single click.